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PLUG FLOW DAIRY DIGESTER CONDITION AFTER 16
YEARS OF OPERATION
Mark
A. Moser and Leo Langerwerf
ABSTRACT
Langerwerf
Dairy is a 400 cow dairy in Durham, California with an RCM plug flow
anaerobic digester that has been in operation continuously since 1982.
By 1997 digester gas production had dropped by about 30% due to
holes in the gas collection bag and loss of volume due to solids
accumulation. This project disassembled the digester, removed
accumulated floating crust and settled sludge, evaluated component
condition, and replaced some components. The digester was refurbished
and restarted at a cost of $50,000.
60 days after the restart electricity production was 50% higher
than before the project began. Findings
after 16 years of operation are: 1) floating crust averaged 4 feet
thick; 2) settled sludge averaged 5.5 feet thick; 3) sludge and crust
occupied 2/3 of the digester volume: 4) the digester only accumulated 1%
of the solids that would be estimated using NRCS sludge accumulation
volume calculations; 5) hypalon gas bag material degraded; 6) there was
minor corrosion of digester concrete and steel; 7) digester service life
estimates can be increased from 20 years to 30 years; 8) total system
operation and maintenance cost is about 4% of total capital costs
annually; and 9) digester operation and maintenance cost is 2.9% of
digester capital costs annually. Major
project costs were removing crust and sludge, new greenhouse parts, and
buying and installing a new gas bag with attachment hardware. The 1981
project cost was $200,000 while the gross value of digester products to
date has been $698,000. Operation
and maintenance costs to date have been $160,000.
The dairy received matching grant assistance from the Western
Regional Biomass Energy Program (WRBEP) to refurbish the digester and
document the process. The
AgSTAR program provided technical assistance.
PROJECT HISTORY
Langerwerf
Dairy is a 400-cow family run dairy in Durham, California with a plug
flow anaerobic digester that has been in operation since 1981. The
anaerobic digester system includes a collection/mix tank with a transfer
pump, a plug flow digester, a post-digester solids separator with solids
storage system and a biogas-fired engine-generator.
A
Caterpillar G3306 engine generator has operated about 90% of the project
lifetime, averaging about 40 kW output.
In 16 years of operation the digester has produced about
3,400,000 m3 (120,000,000 ft3) of biogas 2,000,000 m3 (72,000,000 ft3)
of methane and the engine converted the biogas into 5,000,000 kWh of
electricity. As of January 1999 approximately 17,600 m3 (23,000 yd3) of
digested fiber have been sold.
The
digester, generation and solids separation system cost $200,000 in 1981
Since 1981, the farm spent about $160,000 on operation and
maintenance including this $50,000 project. Annualized operation and
maintenance of the whole system considering a 4% inflation rate is about
4% of capital costs. Since
1981 the system has produced $350,000 worth of electricity;
sold approximately $138,000 of digested fiber; replaced $75,000 of heat with hot water recovered from the
engine; and saved $135,000 in lagoon cleanout costs. The net cash return
for the 16 years of operation is approximately $540,000.
DIGESTER DECONSTRUCTION
After 16 years the digester gas production had
decreased. Leaks in the gas collection cover and solids accumulation
were the suspected cause. The
refurbishing project fieldwork began on October 14, 1998.
The perimeter chain link fence, protective greenhouse (2-layer
clear plastic over galvanized steel hoops) and gas collection cover were
removed over a one-week period.
The
floating crust under the gas collection cover was 3 - 5 feet thick and
supported the weight of a man. About 270 m3 (350 yd3) of crust was
removed by a trackhoe and hauled to cropland with farm dump bed trucks.
This required 2 days and 4 people plus the trackhoe operator.
The
remaining digesting slurry was pumped out, with 152 m3 (40,000 gal)
reserved in a nearby tank for digester startup.
1.5 m (5 ft) of settled sludge was covering the digester floor
and part of the heating system. The black steel hot water heating system
was examined and found to be in good condition.
Approximately
308 m3 (400 yd3) of sandy sludge were in the digester and approximately
254 m3 (330 yd3) were removed using a hydraulic mining technique.
High-pressure hoses using recycled digester water were used to wash
sludge solids to a pump that pumped the mixture to a temporary settling
basin near the digester. Clarified
liquid flowed back to the digester.
Cleaning
out the sludge required about 10 days because several different
approaches were tried, before arriving at the workable solution. The
successful hydraulic mining with recycle required 4 men for 5 days.
The
floating crust and settled solids reduced the usable volume of the
digester by about 66%.
COMPONENTS AND MATERIALS AFTER 16 YEARS OF OPERATION
Once
the digester was emptied all components were inspected for
serviceability.
Gas
collection cover. The hypalon gas collection cover material degraded
and finally failed due to UV weathering.
UV weathering caused pinholes and subsequently biogas and water
infiltrated into the cover fabric creating larger holes and leaks.
Gas
collection cover attachment. Black
flat bar steel, angle iron and galvanized bolts were used to attach the
cover to the concrete tank. Sheet
metal capping installed on the top of the digester wall had rusted away.
The atmosphere inside the greenhouse is moist and includes some
hydrogen sulfide volatilized from the effluent end of the digester. Some
manure had run between the cover and the digester wall and remained in
contact with the bolts for many years.
At least a dozen bolt heads had corroded enough to require
drilling out. Some of the flat bar steel had corroded because it was
left in contact with manure and air.
Most of the angle iron was rusty but not corroded significantly.
New hardware was used for cover reattachment.
Concrete.
Some concrete corrosion was found in the same areas
as the cover attachment corrosion and is attributed to manure that had
run along the concrete wall. The
manure decomposed forming acids that etched away one eighth to one
quarter of an inch of concrete over a 12 m (40 ft) length of wall. The corrosion presented no problem with the digester
operation.
Liner
material. Hypalon material was used for the digester liner.
The material was judged to be suitable for continued service.
It was aged and grainy in spots but did not exhibit the holes or
liquid infiltration. No
buildup of struvite was found.
Heat
exchanger and pipe. The
digester heat exchanger was constructed of black steel.
It was found partially buried in sandy sludge and judged to be
not fully effective. Upon
removal of the sludge no external corrosion was found.
Gas
collection pipe. No degradation of any PVC plastic including the gas
collection pipe was found. The
gas intake where the cover rested was slightly deformed, probably due to
16 years of the cover resting on it and being exposed to high
temperatures. There was some accumulation of manure solids evident in
the gas line probably from foaming during startup.
Greenhouse
components.
Galvanized greenhouse support hoops were mildly corroded at unprotected
welds. The corrosion can be attributed to condensation mixed with some
hydrogen sulfide. The hoops
were replaced. The
greenhouse plastic was 4 - 5 years old, at the end of its useful life,
and was replaced.
RESTARTING THE DIGESTER
A
pipe coupling in the heating system was broken during the cleanout
process and later was repaired. The
digester was refilled on 10/22/98 with new and old manure.
Heating began on 10/23 with the engine-generator running on
propane. The new digester
cover was installed using new steel and bolts on 10/28. On 10/29 the
digester temperature was at 29o C
(85o F) and 5% new manure was added.
The digester gas meter was installed and the biogas gas tested in
a flame test the same day. The
flame was consistent and had good color characteristics.
Late on 10/29 the biogas was tested in the engine.
Full power was demonstrated and therefore the engine was set at
20 kW and run continuously on biogas.
Table 1 shows the log of the startup of the digester.
By 11/1 the
engine was running continuously at 30 kW, consuming
544 m3/d (19,200 ft3/d). The
greenhouse was installed mid November to protect the digester during
winter weather. On 11/30
engine output reached 52 kW at continuous operation.
CURRENT OPERATIONS
Digester operation and gas production improved after
startup as the digester acclimated and reached full feed.
Engine-generator operations improved as well and by January of 1999, the
engine was operating at 55 kW. At
the end of 1999 the engine was operating continuously at 62 kW.
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Date
|
Cumulative
Gas
Meter Reading
m3 ft3
|
Average
output since last reading
m3/d ft3/d
|
Effluent
Temp
–
oC oF
|
Effluent
pH
|
|
November
3
|
2,720 (96,000)
|
544 (19,200)
|
34.4
(94)
|
7.3
|
|
5
|
4,572 (161,400)
|
914 (32,280)
|
|
|
|
7
|
5,924 (209,100)
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676 (23,850)
|
38.3
(101)
|
7.4
|
|
9
|
7,300 (257,700)
|
688 (24,300)
|
38.8
(102)
|
7.4
|
|
17
|
14,297
(504,700)
|
875 (30,875)
|
|
|
|
18
|
15,252 (538,400)
|
955 (33,700)
|
39.4
(103)
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7.4
|
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27
|
24,476 (864,000)
|
1,025 (36,178)
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Table
2 shows the farm electricity purchases in September, October, and
November 1997 and 1998.
In 1997 the farm purchased 118-225 kWh/d.
In September 1998 the engine-generator was shut down and the farm
required 609 kWh of electricity per day. November 1998 saw
biogas production increase and electricity purchases decrease to
109 kW/d. The digester
electricity production saved the farm $850 in October alone.
The 1998 purchases can be compared with the 1997 purchases and it
can be seen that even with just startup operation, the farm is buying
less electricity that in 1997. At
the same time, the digester system produced about 1000 surplus kWh in
November 1998 that were sold to PG&E for $356.27.
The farm was not selling nearly as much electricity in 1997.
Table 2. Electricity Purchases Comparison 1997-8
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Month
|
1997 kWh/d purchase
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1998 kWh/d purchase
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September
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194*
|
609**
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|
October
|
118*
|
502***
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November
|
221*
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109*
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* -
generator operating, ** - generator not operating, ***- partial
operation
EXPECTED COMPONENT LIFE
The
project life was expected to be 20 years, based on the usable life of
components in agricultural waste
systems. However, review of
components in place showed most components should continue to function
for at least 10 more years. Table 3 summarizes the expected life of components based on
what has been learned from the project.
REFURBISHING EXPENDITURES
The
project was completed on time and on budget.
Table 4 summarizes the actual expenditures. The situation found
upon opening the digester necessitated altering some strategies and
planned work. Hired labor
was substituted for a contractor when it was obvious that mantime was
more necessary than skilled construction assistance.
Savings were used to spend more money on rental equipment for
removing crust and settled solids. A trackhoe to remove crust saved
money that was then used to hydraulically mine solids.
AgSTAR assistance substituted for some of the planned farm
personnel time. AgSTAR
personnel suggested the recycle settling ponds, set up the cover for
installation and worked with the cover installation crew.
Table
3. Original Component Life
Estimate vs. Revised Estimate of Usable Component Life
|
Component
|
1982 Projected Life
|
1998 Remaining Life
|
Revised Estimate of usable life
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Concrete
|
20
years
|
10+
years
|
30+
years
|
|
Steel
plumbing
|
20
years
|
10+
years
|
30+
years
|
|
Plastic
plumbing
|
20
years
|
10+
years
|
30+
years
|
Greenhouse plastic
|
3
years
|
0
|
4
years
|
|
Greenhouse
galvanized steel
|
20
years
|
4
years
|
20
years
|
|
Gas
collection bag
|
20
years
|
0
|
12
years
|
|
Engine
– between overhauls
|
2
years
|
4
years
|
4
years
|
|
Gas
meter
|
10
years
|
10
years
|
10
years
|
|
Gas
pump
|
5
years
|
4
years
|
4
years
|
|
Project
life
|
20
years
|
10+
years
|
30+
years
|
Table 4. Costs of
Refurbishing the Digester
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Labor
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Costs
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Tasks
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Hours
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$ per unit
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Total
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Disassemble
system
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Farm
Labor
|
hours
|
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213
|
$ 22.00
|
$ 4,686.00
|
|
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Hired
Labor
|
hours
|
|
210
|
$ 12.00
|
$ 2,520.00
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Rent
Mixer/Pumps
|
days
|
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$ 75.00
|
$ 1,084.30
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Rental
crane
|
days
|
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$ 375.00
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$
920.00
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Farm
truck /tractor
|
hours
|
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40
|
$ 25.00
|
$ 1,000.00
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Put
system back together
|
|
|
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Farm
Labor
|
hours
|
|
156
|
$ 22.00
|
$ 3,432.00
|
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Hired
Labor
|
hours
|
|
151
|
$ 12.00
|
$ 1,812.00
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Consulting
|
|
|
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AgSTAR
|
|
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$ 9,800.00
|
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Project
Manager
|
hours
|
|
100
|
$ 65.00
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$ 6,500.00
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Materials
|
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meter
|
Roots
|
|
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$ 1,250.00
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|
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flare
|
Varec
or equiv
|
|
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$ 2,833.71
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cover
|
30
mill polypropylene
|
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$ 4,603.71
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